4th Gear Slip under load
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Re: 4th Gear Slip under load
What is your Shift completion delay set to? Is it still 304 milliseconds as in your last MSQ? That's how long the clutch outputs are supposed to be active for. In your log it only appears to be high for ~ 100 msec or less. I don't see anything obviously wrong in the code, so I will have to dig a bit deeper.
Lance.
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Re: 4th Gear Slip under load
Here is some test code:
This code has a potential fix (though I didn't find anything obviously wrong in the code), but also has some diagnostic channels built in so if it doesn't work a datalog will show what's going on much better and it will be simpler to fix. I will be trying it here. If you were willing to give it a try and post some feedback, that would be great.
Lance.
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Re: 4th Gear Slip under load
Actually, don't other with the code above, it won't help. But I do see the issue in the code now. I just have to fix it...
Lance.
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Re: 4th Gear Slip under load
Okay, here is code that works for me:
(uses INI above)
The problem turned out to be something simple (and stupid!). The delays were x10 in the INI, but this wasn't account for in the code, so they were only 1/10th as long as they should have been. This was a careless mistake on my part, and I apologize for the hassle it has caused you.
As always, thanks for spotting this and bringing it to our attention!
Lance.
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Re: 4th Gear Slip under load
Lance, the code you posted works perfect, and my 2nd spare port (the shift solenoid for 4th gear) is actually working now!
The clutch smoothness (Spare port 1) is still not functioning at all, but TunerStudio claims that it is working fine.
My car just died on the side of the road because I forgot to clean my Megasquirt, so I am inspecting and thoroughly cleaning my Megashift as well. There was some excess flux here and there, so we'll see if that was an issue.
Sam
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Re: 4th Gear Slip under load
I just looked at spare port 1 on my bench using the latest beta code (5.096). It was set up as a selective clutch output, and the gear changes were set up to all 'ON' under 'Shift Output Patterns -> Clutch Pattern (SP1/Output7)'. When I do this, the trace on my scope matches the PWM pattern set under 'Spare Ports -> Spare Port 1 PWM Setup/Percent/Index' (you should make sure these are all set appropriately for your application, of course).
So try the latest beta code here: http://www.msgpio.com/manuals/mshift/V5code.html
If that still doesn't work for you, post your MSQ file and a datalog. You might also want to check the PT7/VB1 jumper for a good connection at both ends (recall this is one of the wire jumpers on the 25x2 header that you added early in the build). Also check the soldering of the VB1 circuit, including the resistor R1; and check the soldering on the AMP seal connector pin 11 as well. You might also check the continuity from the harness side of the ampseal connector (pin 11) to your device (or its connector) to verify that there is less than 1 ohms resistance.
Lance.
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Re: 4th Gear Slip under load
Will do, thanks.
Sam
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Re: 4th Gear Slip under load
Okay, all problems fixed, then transmission broke
I must have been very tired when I re-soldered the TIP120s because the new ones were not on right lol. I re-soldered everything and all clutch inputs worked, and transmission shifted perfectly.
So I turned up the boost... And the 01M disagreed... and broke
MY FAULT, the trans will be rebuilt and probably live to see more MegaShifting on an N/A 16V in a few months
That is all, thank you for all the support
Summary:
-Trans slipped due to a stuck on spare port shift solenoid, because of 2 bad TIP120s
-Once TIP120s were replaced everything worked seamlessly
-01M broke after ~15PSI on my 16V 2.0
Sam
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- Posts: 1696
- Joined: Fri Apr 04, 2008 1:28 pm
Re: 4th Gear Slip under load
Thanks for the feedback. That's too bad about the trans. I know from experience how frustrating that is. I hope your fix will be as quick and painless as possible for you!
Lance.